You are reading
- March 2007 – Wiring was all checked. Coil and Ballast resistor were replaced. {electrical things were not really working right as I was about to find out in a while}. Steering return pipe replaced. Exhaust tail pipe was patched/repaired where it connected to the muffler. LHM was replaced and filters cleaned.
- May 2007 – Electrical connections in engine bay all checked and high tension leads replaced. [following sudden break down in the middle of Sydney city traffic and subsequent towing]
- May 2007 – 6 days later - Ignition was replaced with 123 ignition system
- December 2007 – Both rear suspension boots and pivot balls replaced, and knuckles cleaned and regreased and holding pins retensioned.